I'm using the Grizzly part number because the House of Tools one is just too long. And it's big brother with the horizontal mill, the G3617 under a different part number, is still available from Grizzly.
I'll try to make this thread about the conversion process of this sort of mill. Bare in mind that I have a foundry and that part of my day job involves PC board design and software. So what I might imply is simple, is because it's simple to me.
I have a JGRO (MDF and roller skate bearings) CNC router with stepper motors. I don't really like them. So noisy but they are easy to install and work with.
Initially I put a 500 oz-in motor with 3:1 reduction on the knee. The sloppy fit of the hand crank and almost dropping it on my toes once was the initial reason for the conversion. I ran it with a Gecko Stepper drive and 60V power supply. It became very clear that 500 oz-in wasn't enough so I upgraded to just over 900 oz-in. Oh and I used one of my prototype ELS controllers as the stepper control for motion. No more hand cranking.
Controlling the knee wasn't nearly as simple as one might think. it's a right angle drive to a bevel gear set to turn the ACME screw that lowers and raises a very heavy assembly what with the rotating table arrangement (w/o a horizontal drive capability). And one set of bearings were just cast iron plus there was a lot of backlash on the gears. Running this shaft at high speeds would clearly result in a lot of wear.
So the first step was to place a ball bearing at the bevel gear end and adding a bearing at the crank end. End play was set up at the bevel end for best contact and as little backlash as possible.
So I replaced the iron bushing with the carrier shown in the KneeBackBearingHolder photo.
At the front end I added a casting that held a bearing. It was just short enough to fit on the lathe for boring the slip fit for the ball bearing. The closeup shows two bolts holding it in place and the cover just sitting above on the table.
A second casting held the motor.
The pulley slides over the shaft and 4 bolts anchor it on the 4 flats where the original handle fit so badly.
I'll try to make this thread about the conversion process of this sort of mill. Bare in mind that I have a foundry and that part of my day job involves PC board design and software. So what I might imply is simple, is because it's simple to me.
I have a JGRO (MDF and roller skate bearings) CNC router with stepper motors. I don't really like them. So noisy but they are easy to install and work with.
Initially I put a 500 oz-in motor with 3:1 reduction on the knee. The sloppy fit of the hand crank and almost dropping it on my toes once was the initial reason for the conversion. I ran it with a Gecko Stepper drive and 60V power supply. It became very clear that 500 oz-in wasn't enough so I upgraded to just over 900 oz-in. Oh and I used one of my prototype ELS controllers as the stepper control for motion. No more hand cranking.
Controlling the knee wasn't nearly as simple as one might think. it's a right angle drive to a bevel gear set to turn the ACME screw that lowers and raises a very heavy assembly what with the rotating table arrangement (w/o a horizontal drive capability). And one set of bearings were just cast iron plus there was a lot of backlash on the gears. Running this shaft at high speeds would clearly result in a lot of wear.
So the first step was to place a ball bearing at the bevel gear end and adding a bearing at the crank end. End play was set up at the bevel end for best contact and as little backlash as possible.
So I replaced the iron bushing with the carrier shown in the KneeBackBearingHolder photo.
At the front end I added a casting that held a bearing. It was just short enough to fit on the lathe for boring the slip fit for the ball bearing. The closeup shows two bolts holding it in place and the cover just sitting above on the table.
A second casting held the motor.
The pulley slides over the shaft and 4 bolts anchor it on the 4 flats where the original handle fit so badly.